Will finally get to do some multimeter testing on my ECU tomorrow or Monday as I've got a long weekend due to a national holiday.
Was on the expressway though and floored it in 5th. As soon as it got spooling is was heading way up to 1bar/15psi and I had to get out of it. Could be a sticky actuator or duff boost controller but I'll find that out in time. No fuel cut though. One thing I did notice was that the stock boost gauge only starts to show any movement at all once I'm already in boost. What I mean is that the needle is nowhere near 0 on the stock boost gauge until I'm at least at 3-4psi. Is this normal for the stock boost gauge or should it be a little more accurate than that?
Will test voltages tomorrow and see what results I get.
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