Quote:
Originally Posted by infernosg
It turns out 3/4 wires in the sub-harness connector were wired incorrectly. After de-pinning and correctly re-pinning that connector there's continuity from the ECU to the injector. Just to be sure I also went back and checked the ignition wires. Fortunately those are all good.
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Hmmm. . Mine was that exact same way!
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1993 Yamaha GTS1000
1992 Celica Turbo AllTrac
1987 RX7 Sport
1979 Yamaha G1, KM24 powered
1975 Dolmar KMS4
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