and here it is installed. This is where i found the coolant drain plug loose! damnit the only 2 things i didnt check came back to bite me in the ass. Once it was tightened and my tool installed ops check GOOD.
once again on to finish breakin mileage. at this point it was about 6-7 hundred into it so time to give it more RPM to 6k and a couple pounds of boost 3-5max. This is where i started having problems with the sequential system. So long story short i believe i had every single seq boost problem on the forums and still couldnt get it t work right. I mean i checked everything replaced some solenoids re route vac lines so on and so forth. Now i planned on going single later anyway so... out with all the seq for poor man non-seq. hurray much simpler works as advertised. This was at about 850-9 mileage and i was sick of working on it and wanted boost and it to work.
in my book my break in was done at that point so once i made a HOME DEPOT manual boost controller to mantain 10 PSI i was in it to win it!
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up to this point it has all been to make my newly aquired FD run in a stock fashion.
Now its on to start making it MY OWN performing road car.
TRANS BRACE:
First things first i was missing the 3rd gear shift as for some reason the trans tail shaft was flexing quit a bit. So the fix I decided to use was a transmision brace that i made being i had the material and ability. once installed it made a WORLD of difference in drivability, especially running an ACT solid 6-puck.

EXHAUST:
Of course i wanted to do an exhaust as i was still running a stock cat and some redneck catback. I then decided to do a 4" setup although i knew it would be loud i did not know how loud. i picked up some 4" bends and started running it from the 3" twins downpipe by necking it up to a 4" v-band.
then ran it back to a magnaflow 4" oval race muffler to a single 4"inlet dual 3" outlet flowmaster super 50 hd. Reason being i still wanted a slightly covert twin exit at the rear yet still be able to flow. at this time i picked up a banzia/pineapple rear diff brace(the one that will clear a 4" pipe) and installed it being i was there already.

TWINS:
Now that i had a rather free flowing exhaust i was experiencing boost creap as the stock wastegate was not flowing enough. I removed and disassembled then to port the wastegate unfortunatly my air compressor istoo small to run my die grinder so i ended up doing it with a dremmel. i dont have any pics of it but i opened it up to the outer edges of the flapper door and it know maintains boost perfectly with the large exhaust.